Complaints & Recalls
Official Safety Recalls - Important!
2 RecallsThese are official manufacturer recalls ordered by NHTSA for safety defects. If you own this vehicle, contact your dealer immediately for free repairs.
Kia Motors America
Safety Issue:
Kia Motors America (Kia) is recalling certain 2020-2021 Soul, and 2021 Seltos vehicles equipped with 2.0L Nu MPI engines. The piston oil rings may not have been properly heat-treated, which may result in engine damage.
Potential Risk:
FREE Recall Solution:
Additional Details:
Owners may also contact the National Highway Traffic Safety Administration Vehicle Safety Hotline at 1-888-327-4236 (TTY 1-800-424-9153), or go to www.safercar.gov.
Mfg Campaign: SC209
Recall Date: Apr 13, 2021
Consumer Complaints
394 ComplaintsKia America, Inc.
Defect Description:
STEERING
Potential Consequences:
THE STEERING WHEEL LOCKED AND I WAS UNABLE TO TURN THE ENGINE KEY AROUND. I WAS UNABLE TO START THE CAR AS THE STEERING WHEEL WAS JAMMED. IT TOOK ME OVER 1 HRS TO FINALLY UNNAMED THE STEERING WHEEL. THIS HAS HAPPENED TWICE.
Corrective Action:
THE STEERING WHEEL LOCKED AND I WAS UNABLE TO TURN THE ENGINE KEY AROUND. I WAS UNABLE TO START THE CAR AS THE STEERING WHEEL WAS JAMMED. IT TOOK ME OVER 1 HRS TO FINALLY UNNAMED THE STEERING WHEEL. THIS HAS HAPPENED TWICE.
Additional Notes:
THE STEERING WHEEL LOCKED AND I WAS UNABLE TO TURN THE ENGINE KEY AROUND. I WAS UNABLE TO START THE CAR AS THE STEERING WHEEL WAS JAMMED. IT TOOK ME OVER 1 HRS TO FINALLY UNNAMED THE STEERING WHEEL. THIS HAS HAPPENED TWICE.
Mfg Campaign: 11415772
Recall Date: May 10, 2021
Kia America, Inc.
Defect Description:
POWER TRAIN
Potential Consequences:
WE PURCHASED A 2020 KIA SOUL IN JANUARY 2020, WITH 11 MILES ON IT. EVERYTHING WAS FINE FOR THE FIRST FEW MONTHS, UNTIL ONE DAY MY WIFE WAS DRIVING AT ABOUT 40 MILES AN HOUR AND WAS SLOWING DOWN TO TAKE A RIGHT TURN, THE STEERING WHEEL LOCKED UP AND SHE ALMOST WRECKED, THANKFULLY SHE JERKED THE WHEEL HARD ENOUGH TO BREAK IT LOOSE, BUT IN DOING SO THE SPEEDO CLUSTER GLAD SHATTERED. IT WAS FIXED BUT THE DEALERSHIP TRIED TO BLAME US SAYING SOMEONE HAD TO OF PUNCHED IT. BUT WHEN LOOKING AT THE GLASS CLUSTER IT'S OBVIOUS THAT NOT EVEN A BABY'S HAND COULD FIT DOWN INTO THE CLUSTER TO HIT THE GLASS. THEN AT 20K MILES ALMOST EXACTLY, THE TRANSMISSION WENT OUT, AGAIN THE DEALERSHIP TOOK CARE OF IT, TOOK ABOUT 2 WEEKS FOR A NEW TRANSMISSION. IT STARTED REVVING UP AND WOULD JERK LIKE IT WAS BEING DOWN SHIFTED WHILE GOING DOWN THE HIGHWAY AT 70 MPH. SINCE THEN WE'VE PUT ABOUT 9K MILES ON THE NEW TRANSMISSION AND IS DOING THE SAME THING AGAIN. THE DEALERSHIP TOLD ME THERE WAS 2 RECALLS ON THE VEHICLE FOR THE TRANSMISSION WHEN IT FIRST HAPPENED, ONE WAS FOR AN ELECTRONIC UPDATE, THE OTHER WAS FOR THE ACTUAL TRANSMISSION, BUT I HAVEN'T SEEN ANY RECALLS POSTED, THIS IS THE WORST NEW CAR I'VE EVER OWNED
Corrective Action:
WE PURCHASED A 2020 KIA SOUL IN JANUARY 2020, WITH 11 MILES ON IT. EVERYTHING WAS FINE FOR THE FIRST FEW MONTHS, UNTIL ONE DAY MY WIFE WAS DRIVING AT ABOUT 40 MILES AN HOUR AND WAS SLOWING DOWN TO TAKE A RIGHT TURN, THE STEERING WHEEL LOCKED UP AND SHE ALMOST WRECKED, THANKFULLY SHE JERKED THE WHEEL HARD ENOUGH TO BREAK IT LOOSE, BUT IN DOING SO THE SPEEDO CLUSTER GLAD SHATTERED. IT WAS FIXED BUT THE DEALERSHIP TRIED TO BLAME US SAYING SOMEONE HAD TO OF PUNCHED IT. BUT WHEN LOOKING AT THE GLASS CLUSTER IT'S OBVIOUS THAT NOT EVEN A BABY'S HAND COULD FIT DOWN INTO THE CLUSTER TO HIT THE GLASS. THEN AT 20K MILES ALMOST EXACTLY, THE TRANSMISSION WENT OUT, AGAIN THE DEALERSHIP TOOK CARE OF IT, TOOK ABOUT 2 WEEKS FOR A NEW TRANSMISSION. IT STARTED REVVING UP AND WOULD JERK LIKE IT WAS BEING DOWN SHIFTED WHILE GOING DOWN THE HIGHWAY AT 70 MPH. SINCE THEN WE'VE PUT ABOUT 9K MILES ON THE NEW TRANSMISSION AND IS DOING THE SAME THING AGAIN. THE DEALERSHIP TOLD ME THERE WAS 2 RECALLS ON THE VEHICLE FOR THE TRANSMISSION WHEN IT FIRST HAPPENED, ONE WAS FOR AN ELECTRONIC UPDATE, THE OTHER WAS FOR THE ACTUAL TRANSMISSION, BUT I HAVEN'T SEEN ANY RECALLS POSTED, THIS IS THE WORST NEW CAR I'VE EVER OWNED
Additional Notes:
WE PURCHASED A 2020 KIA SOUL IN JANUARY 2020, WITH 11 MILES ON IT. EVERYTHING WAS FINE FOR THE FIRST FEW MONTHS, UNTIL ONE DAY MY WIFE WAS DRIVING AT ABOUT 40 MILES AN HOUR AND WAS SLOWING DOWN TO TAKE A RIGHT TURN, THE STEERING WHEEL LOCKED UP AND SHE ALMOST WRECKED, THANKFULLY SHE JERKED THE WHEEL HARD ENOUGH TO BREAK IT LOOSE, BUT IN DOING SO THE SPEEDO CLUSTER GLAD SHATTERED. IT WAS FIXED BUT THE DEALERSHIP TRIED TO BLAME US SAYING SOMEONE HAD TO OF PUNCHED IT. BUT WHEN LOOKING AT THE GLASS CLUSTER IT'S OBVIOUS THAT NOT EVEN A BABY'S HAND COULD FIT DOWN INTO THE CLUSTER TO HIT THE GLASS. THEN AT 20K MILES ALMOST EXACTLY, THE TRANSMISSION WENT OUT, AGAIN THE DEALERSHIP TOOK CARE OF IT, TOOK ABOUT 2 WEEKS FOR A NEW TRANSMISSION. IT STARTED REVVING UP AND WOULD JERK LIKE IT WAS BEING DOWN SHIFTED WHILE GOING DOWN THE HIGHWAY AT 70 MPH. SINCE THEN WE'VE PUT ABOUT 9K MILES ON THE NEW TRANSMISSION AND IS DOING THE SAME THING AGAIN. THE DEALERSHIP TOLD ME THERE WAS 2 RECALLS ON THE VEHICLE FOR THE TRANSMISSION WHEN IT FIRST HAPPENED, ONE WAS FOR AN ELECTRONIC UPDATE, THE OTHER WAS FOR THE ACTUAL TRANSMISSION, BUT I HAVEN'T SEEN ANY RECALLS POSTED, THIS IS THE WORST NEW CAR I'VE EVER OWNED
Mfg Campaign: 11414903
Recall Date: May 3, 2021
Kia America, Inc.
Defect Description:
FORWARD COLLISION AVOIDANCE: ADAPTIVE CRUISE CONTROL
Potential Consequences:
WE PURCHASED A 2020 KIA SOUL IN JANUARY 2020, WITH 11 MILES ON IT. EVERYTHING WAS FINE FOR THE FIRST FEW MONTHS, UNTIL ONE DAY MY WIFE WAS DRIVING AT ABOUT 40 MILES AN HOUR AND WAS SLOWING DOWN TO TAKE A RIGHT TURN, THE STEERING WHEEL LOCKED UP AND SHE ALMOST WRECKED, THANKFULLY SHE JERKED THE WHEEL HARD ENOUGH TO BREAK IT LOOSE, BUT IN DOING SO THE SPEEDO CLUSTER GLAD SHATTERED. IT WAS FIXED BUT THE DEALERSHIP TRIED TO BLAME US SAYING SOMEONE HAD TO OF PUNCHED IT. BUT WHEN LOOKING AT THE GLASS CLUSTER IT'S OBVIOUS THAT NOT EVEN A BABY'S HAND COULD FIT DOWN INTO THE CLUSTER TO HIT THE GLASS. THEN AT 20K MILES ALMOST EXACTLY, THE TRANSMISSION WENT OUT, AGAIN THE DEALERSHIP TOOK CARE OF IT, TOOK ABOUT 2 WEEKS FOR A NEW TRANSMISSION. IT STARTED REVVING UP AND WOULD JERK LIKE IT WAS BEING DOWN SHIFTED WHILE GOING DOWN THE HIGHWAY AT 70 MPH. SINCE THEN WE'VE PUT ABOUT 9K MILES ON THE NEW TRANSMISSION AND IS DOING THE SAME THING AGAIN. THE DEALERSHIP TOLD ME THERE WAS 2 RECALLS ON THE VEHICLE FOR THE TRANSMISSION WHEN IT FIRST HAPPENED, ONE WAS FOR AN ELECTRONIC UPDATE, THE OTHER WAS FOR THE ACTUAL TRANSMISSION, BUT I HAVEN'T SEEN ANY RECALLS POSTED, THIS IS THE WORST NEW CAR I'VE EVER OWNED
Corrective Action:
WE PURCHASED A 2020 KIA SOUL IN JANUARY 2020, WITH 11 MILES ON IT. EVERYTHING WAS FINE FOR THE FIRST FEW MONTHS, UNTIL ONE DAY MY WIFE WAS DRIVING AT ABOUT 40 MILES AN HOUR AND WAS SLOWING DOWN TO TAKE A RIGHT TURN, THE STEERING WHEEL LOCKED UP AND SHE ALMOST WRECKED, THANKFULLY SHE JERKED THE WHEEL HARD ENOUGH TO BREAK IT LOOSE, BUT IN DOING SO THE SPEEDO CLUSTER GLAD SHATTERED. IT WAS FIXED BUT THE DEALERSHIP TRIED TO BLAME US SAYING SOMEONE HAD TO OF PUNCHED IT. BUT WHEN LOOKING AT THE GLASS CLUSTER IT'S OBVIOUS THAT NOT EVEN A BABY'S HAND COULD FIT DOWN INTO THE CLUSTER TO HIT THE GLASS. THEN AT 20K MILES ALMOST EXACTLY, THE TRANSMISSION WENT OUT, AGAIN THE DEALERSHIP TOOK CARE OF IT, TOOK ABOUT 2 WEEKS FOR A NEW TRANSMISSION. IT STARTED REVVING UP AND WOULD JERK LIKE IT WAS BEING DOWN SHIFTED WHILE GOING DOWN THE HIGHWAY AT 70 MPH. SINCE THEN WE'VE PUT ABOUT 9K MILES ON THE NEW TRANSMISSION AND IS DOING THE SAME THING AGAIN. THE DEALERSHIP TOLD ME THERE WAS 2 RECALLS ON THE VEHICLE FOR THE TRANSMISSION WHEN IT FIRST HAPPENED, ONE WAS FOR AN ELECTRONIC UPDATE, THE OTHER WAS FOR THE ACTUAL TRANSMISSION, BUT I HAVEN'T SEEN ANY RECALLS POSTED, THIS IS THE WORST NEW CAR I'VE EVER OWNED
Additional Notes:
WE PURCHASED A 2020 KIA SOUL IN JANUARY 2020, WITH 11 MILES ON IT. EVERYTHING WAS FINE FOR THE FIRST FEW MONTHS, UNTIL ONE DAY MY WIFE WAS DRIVING AT ABOUT 40 MILES AN HOUR AND WAS SLOWING DOWN TO TAKE A RIGHT TURN, THE STEERING WHEEL LOCKED UP AND SHE ALMOST WRECKED, THANKFULLY SHE JERKED THE WHEEL HARD ENOUGH TO BREAK IT LOOSE, BUT IN DOING SO THE SPEEDO CLUSTER GLAD SHATTERED. IT WAS FIXED BUT THE DEALERSHIP TRIED TO BLAME US SAYING SOMEONE HAD TO OF PUNCHED IT. BUT WHEN LOOKING AT THE GLASS CLUSTER IT'S OBVIOUS THAT NOT EVEN A BABY'S HAND COULD FIT DOWN INTO THE CLUSTER TO HIT THE GLASS. THEN AT 20K MILES ALMOST EXACTLY, THE TRANSMISSION WENT OUT, AGAIN THE DEALERSHIP TOOK CARE OF IT, TOOK ABOUT 2 WEEKS FOR A NEW TRANSMISSION. IT STARTED REVVING UP AND WOULD JERK LIKE IT WAS BEING DOWN SHIFTED WHILE GOING DOWN THE HIGHWAY AT 70 MPH. SINCE THEN WE'VE PUT ABOUT 9K MILES ON THE NEW TRANSMISSION AND IS DOING THE SAME THING AGAIN. THE DEALERSHIP TOLD ME THERE WAS 2 RECALLS ON THE VEHICLE FOR THE TRANSMISSION WHEN IT FIRST HAPPENED, ONE WAS FOR AN ELECTRONIC UPDATE, THE OTHER WAS FOR THE ACTUAL TRANSMISSION, BUT I HAVEN'T SEEN ANY RECALLS POSTED, THIS IS THE WORST NEW CAR I'VE EVER OWNED
Mfg Campaign: 11414903
Recall Date: May 3, 2021
Kia America, Inc.
Defect Description:
ENGINE
Potential Consequences:
STOPPED AT STOP LIGHT, LIGHT TURNED GREEN. PRESSED GAS AND DASHBOARD SYMBOLS CAME ON AND CAR DIED. TRIED STARTING AGAIN AND IT WAS DEAD. PUSHED IT TO PARKING LOT AND TRIED TO JUMP IT. DIDNT JUMP.. PUSHED TO AUTO ZONE. TESTED BATTERY IT WAS AT 10%. THEY DIDN'T HAVE A BATTERY. USED A JUMP BOX AND CAR STARTED. WAS ABLE TO DRIVE IT HOME.
Corrective Action:
STOPPED AT STOP LIGHT, LIGHT TURNED GREEN. PRESSED GAS AND DASHBOARD SYMBOLS CAME ON AND CAR DIED. TRIED STARTING AGAIN AND IT WAS DEAD. PUSHED IT TO PARKING LOT AND TRIED TO JUMP IT. DIDNT JUMP.. PUSHED TO AUTO ZONE. TESTED BATTERY IT WAS AT 10%. THEY DIDN'T HAVE A BATTERY. USED A JUMP BOX AND CAR STARTED. WAS ABLE TO DRIVE IT HOME.
Additional Notes:
STOPPED AT STOP LIGHT, LIGHT TURNED GREEN. PRESSED GAS AND DASHBOARD SYMBOLS CAME ON AND CAR DIED. TRIED STARTING AGAIN AND IT WAS DEAD. PUSHED IT TO PARKING LOT AND TRIED TO JUMP IT. DIDNT JUMP.. PUSHED TO AUTO ZONE. TESTED BATTERY IT WAS AT 10%. THEY DIDN'T HAVE A BATTERY. USED A JUMP BOX AND CAR STARTED. WAS ABLE TO DRIVE IT HOME.
Mfg Campaign: 11414810
Recall Date: May 2, 2021
Kia America, Inc.
Defect Description:
UNKNOWN OR OTHER
Potential Consequences:
STOPPED AT STOP LIGHT, LIGHT TURNED GREEN. PRESSED GAS AND DASHBOARD SYMBOLS CAME ON AND CAR DIED. TRIED STARTING AGAIN AND IT WAS DEAD. PUSHED IT TO PARKING LOT AND TRIED TO JUMP IT. DIDNT JUMP.. PUSHED TO AUTO ZONE. TESTED BATTERY IT WAS AT 10%. THEY DIDN'T HAVE A BATTERY. USED A JUMP BOX AND CAR STARTED. WAS ABLE TO DRIVE IT HOME.
Corrective Action:
STOPPED AT STOP LIGHT, LIGHT TURNED GREEN. PRESSED GAS AND DASHBOARD SYMBOLS CAME ON AND CAR DIED. TRIED STARTING AGAIN AND IT WAS DEAD. PUSHED IT TO PARKING LOT AND TRIED TO JUMP IT. DIDNT JUMP.. PUSHED TO AUTO ZONE. TESTED BATTERY IT WAS AT 10%. THEY DIDN'T HAVE A BATTERY. USED A JUMP BOX AND CAR STARTED. WAS ABLE TO DRIVE IT HOME.
Additional Notes:
STOPPED AT STOP LIGHT, LIGHT TURNED GREEN. PRESSED GAS AND DASHBOARD SYMBOLS CAME ON AND CAR DIED. TRIED STARTING AGAIN AND IT WAS DEAD. PUSHED IT TO PARKING LOT AND TRIED TO JUMP IT. DIDNT JUMP.. PUSHED TO AUTO ZONE. TESTED BATTERY IT WAS AT 10%. THEY DIDN'T HAVE A BATTERY. USED A JUMP BOX AND CAR STARTED. WAS ABLE TO DRIVE IT HOME.
Mfg Campaign: 11414810
Recall Date: May 2, 2021
Kia America, Inc.
Defect Description:
FORWARD COLLISION AVOIDANCE: WARNINGS
Potential Consequences:
STOPPED AT STOP LIGHT, LIGHT TURNED GREEN. PRESSED GAS AND DASHBOARD SYMBOLS CAME ON AND CAR DIED. TRIED STARTING AGAIN AND IT WAS DEAD. PUSHED IT TO PARKING LOT AND TRIED TO JUMP IT. DIDNT JUMP.. PUSHED TO AUTO ZONE. TESTED BATTERY IT WAS AT 10%. THEY DIDN'T HAVE A BATTERY. USED A JUMP BOX AND CAR STARTED. WAS ABLE TO DRIVE IT HOME.
Corrective Action:
STOPPED AT STOP LIGHT, LIGHT TURNED GREEN. PRESSED GAS AND DASHBOARD SYMBOLS CAME ON AND CAR DIED. TRIED STARTING AGAIN AND IT WAS DEAD. PUSHED IT TO PARKING LOT AND TRIED TO JUMP IT. DIDNT JUMP.. PUSHED TO AUTO ZONE. TESTED BATTERY IT WAS AT 10%. THEY DIDN'T HAVE A BATTERY. USED A JUMP BOX AND CAR STARTED. WAS ABLE TO DRIVE IT HOME.
Additional Notes:
STOPPED AT STOP LIGHT, LIGHT TURNED GREEN. PRESSED GAS AND DASHBOARD SYMBOLS CAME ON AND CAR DIED. TRIED STARTING AGAIN AND IT WAS DEAD. PUSHED IT TO PARKING LOT AND TRIED TO JUMP IT. DIDNT JUMP.. PUSHED TO AUTO ZONE. TESTED BATTERY IT WAS AT 10%. THEY DIDN'T HAVE A BATTERY. USED A JUMP BOX AND CAR STARTED. WAS ABLE TO DRIVE IT HOME.
Mfg Campaign: 11414810
Recall Date: May 2, 2021
Kia America, Inc.
Defect Description:
ENGINE
Potential Consequences:
IN MAY 2020, FOUR MONTHS AFTER LEASING NEW CAR, CAR STALLED WHILE DRIVING IT (WHEEL LOCKED AND ENGINE SHUT DOWN). LUCKILY ONLY ON A RESIDENTIAL ROAD AND NOT HIGHWAY. CAR MADE SLIGHT ENGINE SOUNDS, BUT NO DASHBOARD LIGHTS INDICATORS AT ALL AT ANY POINT.. MANAGED TO DRIVE CAR 10 MINUTES HOME (IT STALLED AGAIN). TOWED CAR TO DEALERSHIP. ENGINE (ONE CYLINDER) HAD TO BE REPLACED WAS TOLD PUT TOGETHER INCORRECTLY AT FACTORY, AND THAT OIL WAS ALMOST COMPLETELY USED UP, ENGINE COULD HAVE EXPLODED. CONFIRMED COULD HAVE STALLED ON HIGHWAY. REPLACED AT NO CHARGE. ASSURED TRANSMISSION FINE AND SAFE TO DRIVE. REPORTED TO KIA CORPORATE RIGHT AWAY AND ASKED THAT CONVERSATION BE RECORDED.. IN APRIL 2021 LEARN OF RECALL FOR SOUL THAT SEEMS TO DESCRIBE THE SAME ISSUE. WENT IN FOR ROUTINE MAINTANENCE, TOLD THAT IT WAS A DIFFERENT PROBLEM AND A DIFFERENT MODEL.
Corrective Action:
IN MAY 2020, FOUR MONTHS AFTER LEASING NEW CAR, CAR STALLED WHILE DRIVING IT (WHEEL LOCKED AND ENGINE SHUT DOWN). LUCKILY ONLY ON A RESIDENTIAL ROAD AND NOT HIGHWAY. CAR MADE SLIGHT ENGINE SOUNDS, BUT NO DASHBOARD LIGHTS INDICATORS AT ALL AT ANY POINT.. MANAGED TO DRIVE CAR 10 MINUTES HOME (IT STALLED AGAIN). TOWED CAR TO DEALERSHIP. ENGINE (ONE CYLINDER) HAD TO BE REPLACED WAS TOLD PUT TOGETHER INCORRECTLY AT FACTORY, AND THAT OIL WAS ALMOST COMPLETELY USED UP, ENGINE COULD HAVE EXPLODED. CONFIRMED COULD HAVE STALLED ON HIGHWAY. REPLACED AT NO CHARGE. ASSURED TRANSMISSION FINE AND SAFE TO DRIVE. REPORTED TO KIA CORPORATE RIGHT AWAY AND ASKED THAT CONVERSATION BE RECORDED.. IN APRIL 2021 LEARN OF RECALL FOR SOUL THAT SEEMS TO DESCRIBE THE SAME ISSUE. WENT IN FOR ROUTINE MAINTANENCE, TOLD THAT IT WAS A DIFFERENT PROBLEM AND A DIFFERENT MODEL.
Additional Notes:
IN MAY 2020, FOUR MONTHS AFTER LEASING NEW CAR, CAR STALLED WHILE DRIVING IT (WHEEL LOCKED AND ENGINE SHUT DOWN). LUCKILY ONLY ON A RESIDENTIAL ROAD AND NOT HIGHWAY. CAR MADE SLIGHT ENGINE SOUNDS, BUT NO DASHBOARD LIGHTS INDICATORS AT ALL AT ANY POINT.. MANAGED TO DRIVE CAR 10 MINUTES HOME (IT STALLED AGAIN). TOWED CAR TO DEALERSHIP. ENGINE (ONE CYLINDER) HAD TO BE REPLACED WAS TOLD PUT TOGETHER INCORRECTLY AT FACTORY, AND THAT OIL WAS ALMOST COMPLETELY USED UP, ENGINE COULD HAVE EXPLODED. CONFIRMED COULD HAVE STALLED ON HIGHWAY. REPLACED AT NO CHARGE. ASSURED TRANSMISSION FINE AND SAFE TO DRIVE. REPORTED TO KIA CORPORATE RIGHT AWAY AND ASKED THAT CONVERSATION BE RECORDED.. IN APRIL 2021 LEARN OF RECALL FOR SOUL THAT SEEMS TO DESCRIBE THE SAME ISSUE. WENT IN FOR ROUTINE MAINTANENCE, TOLD THAT IT WAS A DIFFERENT PROBLEM AND A DIFFERENT MODEL.
Mfg Campaign: 11414270
Recall Date: Apr 28, 2021
Kia America, Inc.
Defect Description:
ENGINE
Potential Consequences:
THE CAR STALLED IN TRAFFIC WHILE I WAS AT A STOP LIGHT. I PUT THE CAR IN PARK, AND THE ENGINE RE-STARTED. THE CAR HAD 6,595 MILES ON THE ODOMETER, AND THE FIRST SERVICE WAS DUE AT 7,500 MILES. AFTER THIS STALLING INCIDENT, IN ORDER TO PREVENT THIS HAPPENING AGAIN, EVERY TIME I HAD TO STOP AFTER THAT, AT A LIGHT OR INTERSECTION, I PUT THE CAR IN PARK. THE NEXT DAY, DRIVING AT 25 MPH ON A CITY STREET, LOUD RATTLING AND METALLIC SOUNDS CAME FROM THE ENGINE. I CHECKED THE OIL. THERE WAS NO TRACE OF OIL ON THE DIPSTICK. I PUT IN 2 QUARTS OF OIL, AND THE DIPSTICK SHOWED THE SUMP WAS NOW FULL. I CHECKED THE TAILPIPE AND FOUND A CARBON DEPOSIT ON THE INSIDE, INDICATING THE BURNING OF OIL. I TOOK THE CAR TO THE DEALERSHIP WHERE I BOUGHT IT - KIRBY KIA IN VENTURA CA - AND THEY DIAGNOSED A SEVERE ENGINE MALFUNCTION WITH EVIDENCE OF METAL SHAVINGS AFTER REMOVING THE VALVE COVER, AND IN THE OIL FILTER. THEY SAID THEY NEEDED TO REPLACE THE ENGINE. THEY PROVIDED ME WITH A COMPLIMENTARY RENTAL CAR FOR 10 DAYS, THEN A LOANER, AND RETURNED MY VEHICLE TO ME AFTER 21 DAYS. IN THE PAPERWORK THEY GAVE ME ON RETURNING MY VEHICLE IT STATES THEY INSTALLED A REMANUFACTURED LONG BLOCK ENGINE AND INTAKE MANIFOLD. AT NO POINT IN THIS WHOLE PROCEDURE WAS I ASKED TO CONSENT TO THE ENGINE BEING REPLACED, AND I SIGNED NO DOCUMENT AUTHORIZING THIS TO BE DONE. AT THE END, I WROTE THAT MY SIGNATURE ONLY INDICATED MY CAR HAD BEEN RETURNED TO ME. NO APOLOGY WAS EXPRESSED TO ME BY KIA FOR THE MAJOR INCONVENIENCE THE FAILURE OF THE ENGINE IN THIS NEW CAR HAD CAUSED ME, EXCEPT WHEN I INFORMED THE MANAGEMENT OF THE DEALERSHIP OF THIS FACT, THEY CALLED ME TO EXPRESS REGRET.
Corrective Action:
THE CAR STALLED IN TRAFFIC WHILE I WAS AT A STOP LIGHT. I PUT THE CAR IN PARK, AND THE ENGINE RE-STARTED. THE CAR HAD 6,595 MILES ON THE ODOMETER, AND THE FIRST SERVICE WAS DUE AT 7,500 MILES. AFTER THIS STALLING INCIDENT, IN ORDER TO PREVENT THIS HAPPENING AGAIN, EVERY TIME I HAD TO STOP AFTER THAT, AT A LIGHT OR INTERSECTION, I PUT THE CAR IN PARK. THE NEXT DAY, DRIVING AT 25 MPH ON A CITY STREET, LOUD RATTLING AND METALLIC SOUNDS CAME FROM THE ENGINE. I CHECKED THE OIL. THERE WAS NO TRACE OF OIL ON THE DIPSTICK. I PUT IN 2 QUARTS OF OIL, AND THE DIPSTICK SHOWED THE SUMP WAS NOW FULL. I CHECKED THE TAILPIPE AND FOUND A CARBON DEPOSIT ON THE INSIDE, INDICATING THE BURNING OF OIL. I TOOK THE CAR TO THE DEALERSHIP WHERE I BOUGHT IT - KIRBY KIA IN VENTURA CA - AND THEY DIAGNOSED A SEVERE ENGINE MALFUNCTION WITH EVIDENCE OF METAL SHAVINGS AFTER REMOVING THE VALVE COVER, AND IN THE OIL FILTER. THEY SAID THEY NEEDED TO REPLACE THE ENGINE. THEY PROVIDED ME WITH A COMPLIMENTARY RENTAL CAR FOR 10 DAYS, THEN A LOANER, AND RETURNED MY VEHICLE TO ME AFTER 21 DAYS. IN THE PAPERWORK THEY GAVE ME ON RETURNING MY VEHICLE IT STATES THEY INSTALLED A REMANUFACTURED LONG BLOCK ENGINE AND INTAKE MANIFOLD. AT NO POINT IN THIS WHOLE PROCEDURE WAS I ASKED TO CONSENT TO THE ENGINE BEING REPLACED, AND I SIGNED NO DOCUMENT AUTHORIZING THIS TO BE DONE. AT THE END, I WROTE THAT MY SIGNATURE ONLY INDICATED MY CAR HAD BEEN RETURNED TO ME. NO APOLOGY WAS EXPRESSED TO ME BY KIA FOR THE MAJOR INCONVENIENCE THE FAILURE OF THE ENGINE IN THIS NEW CAR HAD CAUSED ME, EXCEPT WHEN I INFORMED THE MANAGEMENT OF THE DEALERSHIP OF THIS FACT, THEY CALLED ME TO EXPRESS REGRET.
Additional Notes:
THE CAR STALLED IN TRAFFIC WHILE I WAS AT A STOP LIGHT. I PUT THE CAR IN PARK, AND THE ENGINE RE-STARTED. THE CAR HAD 6,595 MILES ON THE ODOMETER, AND THE FIRST SERVICE WAS DUE AT 7,500 MILES. AFTER THIS STALLING INCIDENT, IN ORDER TO PREVENT THIS HAPPENING AGAIN, EVERY TIME I HAD TO STOP AFTER THAT, AT A LIGHT OR INTERSECTION, I PUT THE CAR IN PARK. THE NEXT DAY, DRIVING AT 25 MPH ON A CITY STREET, LOUD RATTLING AND METALLIC SOUNDS CAME FROM THE ENGINE. I CHECKED THE OIL. THERE WAS NO TRACE OF OIL ON THE DIPSTICK. I PUT IN 2 QUARTS OF OIL, AND THE DIPSTICK SHOWED THE SUMP WAS NOW FULL. I CHECKED THE TAILPIPE AND FOUND A CARBON DEPOSIT ON THE INSIDE, INDICATING THE BURNING OF OIL. I TOOK THE CAR TO THE DEALERSHIP WHERE I BOUGHT IT - KIRBY KIA IN VENTURA CA - AND THEY DIAGNOSED A SEVERE ENGINE MALFUNCTION WITH EVIDENCE OF METAL SHAVINGS AFTER REMOVING THE VALVE COVER, AND IN THE OIL FILTER. THEY SAID THEY NEEDED TO REPLACE THE ENGINE. THEY PROVIDED ME WITH A COMPLIMENTARY RENTAL CAR FOR 10 DAYS, THEN A LOANER, AND RETURNED MY VEHICLE TO ME AFTER 21 DAYS. IN THE PAPERWORK THEY GAVE ME ON RETURNING MY VEHICLE IT STATES THEY INSTALLED A REMANUFACTURED LONG BLOCK ENGINE AND INTAKE MANIFOLD. AT NO POINT IN THIS WHOLE PROCEDURE WAS I ASKED TO CONSENT TO THE ENGINE BEING REPLACED, AND I SIGNED NO DOCUMENT AUTHORIZING THIS TO BE DONE. AT THE END, I WROTE THAT MY SIGNATURE ONLY INDICATED MY CAR HAD BEEN RETURNED TO ME. NO APOLOGY WAS EXPRESSED TO ME BY KIA FOR THE MAJOR INCONVENIENCE THE FAILURE OF THE ENGINE IN THIS NEW CAR HAD CAUSED ME, EXCEPT WHEN I INFORMED THE MANAGEMENT OF THE DEALERSHIP OF THIS FACT, THEY CALLED ME TO EXPRESS REGRET.
Mfg Campaign: 11413629
Recall Date: Apr 24, 2021
Kia America, Inc.
Defect Description:
POWER TRAIN
Potential Consequences:
ON MARCH 2ND. WE WERE DRIVING OUR 2020 KIA SOUL S. WE WERE DRIVING ON I95NORTH. THE RPM'S KEPT PULSING, WE TOOK THE CAR OFF OF CRUISE AND IT SEEMED BETTER FOR A FEW MINUTES. AFTER THE FEW MINUTES THE PULSING RETURNED, GIVING IT THE GAS THE RPM'S WENT UP BUT OUR SPEED WAS SLOWING. WE GOT IN THE INSIDE LANE PLANNING ON GETTING OFF THE NEXT EXIT. THE ENGINE STARTED RACING WITH NO CHANGE IN OUR SPEED. WE GOT OFF AT THE NEXT EXIT STATE ROAD 527 IN SOUTH CAROLINA. WE HAD TO PRACTICALLY FLOOR IT TO GET OFF THE ROAD. WE PULL TO THE SIDE AND CALLED ROADSIDE ASSISTANCE. THE CAR AT THIS POINT HAD 8006 MILES ON IT. WE COULD NOT MOVE THE CAR AT ALL AT THIS POINT. IT TOOK A FEW HOURS, BUT THE CAR WAS TOWED TO THE CLOSET DEALER, IN FLORENCE SC. THE NEXT DAY THE DEALER CHECKED THE CAR AND SAID THE TRANSMISSION HAD FAILED. AT APPROXIMATELY 4:30 PM, THE DEALER CALLED TO LET US KNOW THAT KIA HAD APPROVED SUBSTITUTE TRANSPORTATION. THE FOLLOWING MORNING THE DEALER PICKED US UP AND DROVE US TO GET A VEHICLE. WE UNLOADED MOST OF OUR BELONGINGS FROM OUR CAR TO THE RENTAL AND CONTINUED OUR DELAYED JOURNEY TO MASSACHUSETTS. I HAVE CALLED THE DEALER TWICE, AND LEFT MESSAGES. AFTER THE SECOND CALL, I DID GET A CALL BACK. I WAS TOLD THAT THE REPLACEMENT TRANSMISSION WAS ON BACKORDER AND SHOULD BE DELIVERED MAY 11TH. AFTER READING MANY SIMILAR PROBLEMS ON THIS SITE, THIS IS NOT AN ISOLATED CASE AND IS A DANGEROUS SITUATION. I AM NOW SEEING THAT THE 2020 SOUL HAS AN ENGINE RECALL. OBVIOUSLY THESE VEHICLES HAVE PROBLEMS.
Corrective Action:
ON MARCH 2ND. WE WERE DRIVING OUR 2020 KIA SOUL S. WE WERE DRIVING ON I95NORTH. THE RPM'S KEPT PULSING, WE TOOK THE CAR OFF OF CRUISE AND IT SEEMED BETTER FOR A FEW MINUTES. AFTER THE FEW MINUTES THE PULSING RETURNED, GIVING IT THE GAS THE RPM'S WENT UP BUT OUR SPEED WAS SLOWING. WE GOT IN THE INSIDE LANE PLANNING ON GETTING OFF THE NEXT EXIT. THE ENGINE STARTED RACING WITH NO CHANGE IN OUR SPEED. WE GOT OFF AT THE NEXT EXIT STATE ROAD 527 IN SOUTH CAROLINA. WE HAD TO PRACTICALLY FLOOR IT TO GET OFF THE ROAD. WE PULL TO THE SIDE AND CALLED ROADSIDE ASSISTANCE. THE CAR AT THIS POINT HAD 8006 MILES ON IT. WE COULD NOT MOVE THE CAR AT ALL AT THIS POINT. IT TOOK A FEW HOURS, BUT THE CAR WAS TOWED TO THE CLOSET DEALER, IN FLORENCE SC. THE NEXT DAY THE DEALER CHECKED THE CAR AND SAID THE TRANSMISSION HAD FAILED. AT APPROXIMATELY 4:30 PM, THE DEALER CALLED TO LET US KNOW THAT KIA HAD APPROVED SUBSTITUTE TRANSPORTATION. THE FOLLOWING MORNING THE DEALER PICKED US UP AND DROVE US TO GET A VEHICLE. WE UNLOADED MOST OF OUR BELONGINGS FROM OUR CAR TO THE RENTAL AND CONTINUED OUR DELAYED JOURNEY TO MASSACHUSETTS. I HAVE CALLED THE DEALER TWICE, AND LEFT MESSAGES. AFTER THE SECOND CALL, I DID GET A CALL BACK. I WAS TOLD THAT THE REPLACEMENT TRANSMISSION WAS ON BACKORDER AND SHOULD BE DELIVERED MAY 11TH. AFTER READING MANY SIMILAR PROBLEMS ON THIS SITE, THIS IS NOT AN ISOLATED CASE AND IS A DANGEROUS SITUATION. I AM NOW SEEING THAT THE 2020 SOUL HAS AN ENGINE RECALL. OBVIOUSLY THESE VEHICLES HAVE PROBLEMS.
Additional Notes:
ON MARCH 2ND. WE WERE DRIVING OUR 2020 KIA SOUL S. WE WERE DRIVING ON I95NORTH. THE RPM'S KEPT PULSING, WE TOOK THE CAR OFF OF CRUISE AND IT SEEMED BETTER FOR A FEW MINUTES. AFTER THE FEW MINUTES THE PULSING RETURNED, GIVING IT THE GAS THE RPM'S WENT UP BUT OUR SPEED WAS SLOWING. WE GOT IN THE INSIDE LANE PLANNING ON GETTING OFF THE NEXT EXIT. THE ENGINE STARTED RACING WITH NO CHANGE IN OUR SPEED. WE GOT OFF AT THE NEXT EXIT STATE ROAD 527 IN SOUTH CAROLINA. WE HAD TO PRACTICALLY FLOOR IT TO GET OFF THE ROAD. WE PULL TO THE SIDE AND CALLED ROADSIDE ASSISTANCE. THE CAR AT THIS POINT HAD 8006 MILES ON IT. WE COULD NOT MOVE THE CAR AT ALL AT THIS POINT. IT TOOK A FEW HOURS, BUT THE CAR WAS TOWED TO THE CLOSET DEALER, IN FLORENCE SC. THE NEXT DAY THE DEALER CHECKED THE CAR AND SAID THE TRANSMISSION HAD FAILED. AT APPROXIMATELY 4:30 PM, THE DEALER CALLED TO LET US KNOW THAT KIA HAD APPROVED SUBSTITUTE TRANSPORTATION. THE FOLLOWING MORNING THE DEALER PICKED US UP AND DROVE US TO GET A VEHICLE. WE UNLOADED MOST OF OUR BELONGINGS FROM OUR CAR TO THE RENTAL AND CONTINUED OUR DELAYED JOURNEY TO MASSACHUSETTS. I HAVE CALLED THE DEALER TWICE, AND LEFT MESSAGES. AFTER THE SECOND CALL, I DID GET A CALL BACK. I WAS TOLD THAT THE REPLACEMENT TRANSMISSION WAS ON BACKORDER AND SHOULD BE DELIVERED MAY 11TH. AFTER READING MANY SIMILAR PROBLEMS ON THIS SITE, THIS IS NOT AN ISOLATED CASE AND IS A DANGEROUS SITUATION. I AM NOW SEEING THAT THE 2020 SOUL HAS AN ENGINE RECALL. OBVIOUSLY THESE VEHICLES HAVE PROBLEMS.
Mfg Campaign: 11413596
Recall Date: Apr 23, 2021
Kia America, Inc.
Defect Description:
ENGINE
Potential Consequences:
TL* THE CONTACT OWNS A 2020 KIA SOUL. WHILE DRIVING 35 MPH, THE VEHICLE STALLED WITH THE CHECK ENGINE WARNING LIGHT ILLUMINATED. THE CONTACT STATED THAT THE VEHICLE WAS NOT DRIVING PROPERLY. THE VEHICLE WAS TOWED TO DANBURY KIA (100A FEDERAL RD, DANBURY, CT 06810, (203) 730-5737) AND WAS DIAGNOSED WITH ENGINE DAMAGE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE HOWEVER, PROVIDED NO ASSISTANCE. THE FAILURE MILEAGE WAS 13,706.
Corrective Action:
TL* THE CONTACT OWNS A 2020 KIA SOUL. WHILE DRIVING 35 MPH, THE VEHICLE STALLED WITH THE CHECK ENGINE WARNING LIGHT ILLUMINATED. THE CONTACT STATED THAT THE VEHICLE WAS NOT DRIVING PROPERLY. THE VEHICLE WAS TOWED TO DANBURY KIA (100A FEDERAL RD, DANBURY, CT 06810, (203) 730-5737) AND WAS DIAGNOSED WITH ENGINE DAMAGE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE HOWEVER, PROVIDED NO ASSISTANCE. THE FAILURE MILEAGE WAS 13,706.
Additional Notes:
TL* THE CONTACT OWNS A 2020 KIA SOUL. WHILE DRIVING 35 MPH, THE VEHICLE STALLED WITH THE CHECK ENGINE WARNING LIGHT ILLUMINATED. THE CONTACT STATED THAT THE VEHICLE WAS NOT DRIVING PROPERLY. THE VEHICLE WAS TOWED TO DANBURY KIA (100A FEDERAL RD, DANBURY, CT 06810, (203) 730-5737) AND WAS DIAGNOSED WITH ENGINE DAMAGE. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE HOWEVER, PROVIDED NO ASSISTANCE. THE FAILURE MILEAGE WAS 13,706.
Mfg Campaign: 11413402
Recall Date: Apr 22, 2021
Kia America, Inc.
Defect Description:
ENGINE
Potential Consequences:
ENGINE EXPERIENCED TOTAL FAILURE AT 14,510 MILES. KIA KEPT VEHICLE OVER 60 DAYS AND RETURNED VEHICLE TO ME WITH FURTHER DAMAGE TO BODY
Corrective Action:
ENGINE EXPERIENCED TOTAL FAILURE AT 14,510 MILES. KIA KEPT VEHICLE OVER 60 DAYS AND RETURNED VEHICLE TO ME WITH FURTHER DAMAGE TO BODY
Additional Notes:
ENGINE EXPERIENCED TOTAL FAILURE AT 14,510 MILES. KIA KEPT VEHICLE OVER 60 DAYS AND RETURNED VEHICLE TO ME WITH FURTHER DAMAGE TO BODY
Mfg Campaign: 11413406
Recall Date: Apr 22, 2021
Kia America, Inc.
Defect Description:
POWER TRAIN
Potential Consequences:
THE TRANSMISSION FAILED TWICE THE FIRST TIME THEY REPLACED THE TRANSMISSION AND NOW THEY HAVE TO REPLACE IT AGAIN THEY ARE SAYING . THE VEHICLE WAS ON THE HIGHWAY AND ALL OF THE SUDDEN THE RPMS WENT THROUGH THE ROOF AND THE VEHICLE JUST STARTED TO DIE .
Corrective Action:
THE TRANSMISSION FAILED TWICE THE FIRST TIME THEY REPLACED THE TRANSMISSION AND NOW THEY HAVE TO REPLACE IT AGAIN THEY ARE SAYING . THE VEHICLE WAS ON THE HIGHWAY AND ALL OF THE SUDDEN THE RPMS WENT THROUGH THE ROOF AND THE VEHICLE JUST STARTED TO DIE .
Additional Notes:
THE TRANSMISSION FAILED TWICE THE FIRST TIME THEY REPLACED THE TRANSMISSION AND NOW THEY HAVE TO REPLACE IT AGAIN THEY ARE SAYING . THE VEHICLE WAS ON THE HIGHWAY AND ALL OF THE SUDDEN THE RPMS WENT THROUGH THE ROOF AND THE VEHICLE JUST STARTED TO DIE .
Mfg Campaign: 11408074
Recall Date: Apr 14, 2021
Kia America, Inc.
Defect Description:
POWER TRAIN
Potential Consequences:
WHEN THE AUTOMATIC START STOP START IS ON WHEN I STOP AND THE ENGINE SHUTS OFF AS IT SHOULD, WHEN I RELEASE THE BRAKE IT MAKES A WHINING NOISE FOR A FEW SECONDS. ALSO HAPPENS WHEN GOING UP MY DRIVEWAY. HAVE READ THAT THIS IS HAPPENING IN A LOT OF PEOPLE'S 2020 KIA SOUL'S AND NOBODY SEEMS TO KNOW OR HAVE A FIX.
Corrective Action:
WHEN THE AUTOMATIC START STOP START IS ON WHEN I STOP AND THE ENGINE SHUTS OFF AS IT SHOULD, WHEN I RELEASE THE BRAKE IT MAKES A WHINING NOISE FOR A FEW SECONDS. ALSO HAPPENS WHEN GOING UP MY DRIVEWAY. HAVE READ THAT THIS IS HAPPENING IN A LOT OF PEOPLE'S 2020 KIA SOUL'S AND NOBODY SEEMS TO KNOW OR HAVE A FIX.
Additional Notes:
WHEN THE AUTOMATIC START STOP START IS ON WHEN I STOP AND THE ENGINE SHUTS OFF AS IT SHOULD, WHEN I RELEASE THE BRAKE IT MAKES A WHINING NOISE FOR A FEW SECONDS. ALSO HAPPENS WHEN GOING UP MY DRIVEWAY. HAVE READ THAT THIS IS HAPPENING IN A LOT OF PEOPLE'S 2020 KIA SOUL'S AND NOBODY SEEMS TO KNOW OR HAVE A FIX.
Mfg Campaign: 11407823
Recall Date: Apr 13, 2021
Kia America, Inc.
Defect Description:
UNKNOWN OR OTHER
Potential Consequences:
WHEN THE AUTOMATIC START STOP START IS ON WHEN I STOP AND THE ENGINE SHUTS OFF AS IT SHOULD, WHEN I RELEASE THE BRAKE IT MAKES A WHINING NOISE FOR A FEW SECONDS. ALSO HAPPENS WHEN GOING UP MY DRIVEWAY. HAVE READ THAT THIS IS HAPPENING IN A LOT OF PEOPLE'S 2020 KIA SOUL'S AND NOBODY SEEMS TO KNOW OR HAVE A FIX.
Corrective Action:
WHEN THE AUTOMATIC START STOP START IS ON WHEN I STOP AND THE ENGINE SHUTS OFF AS IT SHOULD, WHEN I RELEASE THE BRAKE IT MAKES A WHINING NOISE FOR A FEW SECONDS. ALSO HAPPENS WHEN GOING UP MY DRIVEWAY. HAVE READ THAT THIS IS HAPPENING IN A LOT OF PEOPLE'S 2020 KIA SOUL'S AND NOBODY SEEMS TO KNOW OR HAVE A FIX.
Additional Notes:
WHEN THE AUTOMATIC START STOP START IS ON WHEN I STOP AND THE ENGINE SHUTS OFF AS IT SHOULD, WHEN I RELEASE THE BRAKE IT MAKES A WHINING NOISE FOR A FEW SECONDS. ALSO HAPPENS WHEN GOING UP MY DRIVEWAY. HAVE READ THAT THIS IS HAPPENING IN A LOT OF PEOPLE'S 2020 KIA SOUL'S AND NOBODY SEEMS TO KNOW OR HAVE A FIX.
Mfg Campaign: 11407823
Recall Date: Apr 13, 2021
Kia America, Inc.
Defect Description:
FUEL/PROPULSION SYSTEM
Potential Consequences:
BOUGHT BRAND NEW. AT 32K MILES (4MONTHS AFTER 30KTUNE UP) ENGINE LIGHT CAME ON. TOOK TO EARNHARDT KIA IN PHX. WHO INITIALLY STATED THERE WAS 'SOMETHING BROKEN IN THE TRANSMISSION' AFTER A FEW HOURS THEY THEN STATED THE CAR HAD 'INTERNALLY OVERHEATED AND THERE WAS COMBUSTIBLE GASES IN THE RADIATOR. THE THERMOSTAT NEVER INDICATED OVERHEATING. COOLANT RESERVOIR WAS BONE DRY (AFTER FILLING IT THE DAY BEFORE). AFTER 31 DAYS AT KIA A NEW HEAD GASKET WAS PUT ON.. THOUGH I WAS TOLD THE CAR WAS GETTING A NEW ENGINE. I ASKED THE DEALER ON EACH CALL... WHAT ABOUT THE TRANSMISSION WHEREAS I WAS TOLD KOA WOULD MAKE SURE EVERYTHING WOULD BE FIXED BEFORE RETURNED. CAR WAS RETURNED TO ME ON 2/21. ON 4/1 AFTER DRIVING 380(+/-) MILES FROM PHX TO SAN DIEGO TO SEE MY MARINE DEPLOY, THE CAR BEGAN TO SURGE, RPMS SKYROCKETED AND CAR BARELY MADE IT UP HILL. SURGING CONTINUED, UNTIL IT BEGAN TO SLIP AND I PULLED OFF THE ROAD AND INTO A SHOPPING CENTER. CAR TOWED TO ESCONDIDO KIA WHO KINDLY GAVE ME A LOANER. NOW BACK IN AZ, I AM TOLD THAT WHEN IT'S FIXED, TRANSPORT TO ME IS UNLIKELY AND IF APPROVED KIA DOES NOT GUARANTEE AGAINST ANY DAMAGE DURING TRANSPORT. ITS A NEW CAR! DUE TO MEDICAL NEEDS HERE, DRIVING 6.5 HOURS THERE AND THEN BACK JUST ISN'T FEASIBLE. KIA DOESNT CARE. I WILL BE OUT OF THIS CAR ASAP AND YOU CAN BET MY NEXT WILL NOT BE A KILLER KIA!
Corrective Action:
BOUGHT BRAND NEW. AT 32K MILES (4MONTHS AFTER 30KTUNE UP) ENGINE LIGHT CAME ON. TOOK TO EARNHARDT KIA IN PHX. WHO INITIALLY STATED THERE WAS 'SOMETHING BROKEN IN THE TRANSMISSION' AFTER A FEW HOURS THEY THEN STATED THE CAR HAD 'INTERNALLY OVERHEATED AND THERE WAS COMBUSTIBLE GASES IN THE RADIATOR. THE THERMOSTAT NEVER INDICATED OVERHEATING. COOLANT RESERVOIR WAS BONE DRY (AFTER FILLING IT THE DAY BEFORE). AFTER 31 DAYS AT KIA A NEW HEAD GASKET WAS PUT ON.. THOUGH I WAS TOLD THE CAR WAS GETTING A NEW ENGINE. I ASKED THE DEALER ON EACH CALL... WHAT ABOUT THE TRANSMISSION WHEREAS I WAS TOLD KOA WOULD MAKE SURE EVERYTHING WOULD BE FIXED BEFORE RETURNED. CAR WAS RETURNED TO ME ON 2/21. ON 4/1 AFTER DRIVING 380(+/-) MILES FROM PHX TO SAN DIEGO TO SEE MY MARINE DEPLOY, THE CAR BEGAN TO SURGE, RPMS SKYROCKETED AND CAR BARELY MADE IT UP HILL. SURGING CONTINUED, UNTIL IT BEGAN TO SLIP AND I PULLED OFF THE ROAD AND INTO A SHOPPING CENTER. CAR TOWED TO ESCONDIDO KIA WHO KINDLY GAVE ME A LOANER. NOW BACK IN AZ, I AM TOLD THAT WHEN IT'S FIXED, TRANSPORT TO ME IS UNLIKELY AND IF APPROVED KIA DOES NOT GUARANTEE AGAINST ANY DAMAGE DURING TRANSPORT. ITS A NEW CAR! DUE TO MEDICAL NEEDS HERE, DRIVING 6.5 HOURS THERE AND THEN BACK JUST ISN'T FEASIBLE. KIA DOESNT CARE. I WILL BE OUT OF THIS CAR ASAP AND YOU CAN BET MY NEXT WILL NOT BE A KILLER KIA!
Additional Notes:
BOUGHT BRAND NEW. AT 32K MILES (4MONTHS AFTER 30KTUNE UP) ENGINE LIGHT CAME ON. TOOK TO EARNHARDT KIA IN PHX. WHO INITIALLY STATED THERE WAS 'SOMETHING BROKEN IN THE TRANSMISSION' AFTER A FEW HOURS THEY THEN STATED THE CAR HAD 'INTERNALLY OVERHEATED AND THERE WAS COMBUSTIBLE GASES IN THE RADIATOR. THE THERMOSTAT NEVER INDICATED OVERHEATING. COOLANT RESERVOIR WAS BONE DRY (AFTER FILLING IT THE DAY BEFORE). AFTER 31 DAYS AT KIA A NEW HEAD GASKET WAS PUT ON.. THOUGH I WAS TOLD THE CAR WAS GETTING A NEW ENGINE. I ASKED THE DEALER ON EACH CALL... WHAT ABOUT THE TRANSMISSION WHEREAS I WAS TOLD KOA WOULD MAKE SURE EVERYTHING WOULD BE FIXED BEFORE RETURNED. CAR WAS RETURNED TO ME ON 2/21. ON 4/1 AFTER DRIVING 380(+/-) MILES FROM PHX TO SAN DIEGO TO SEE MY MARINE DEPLOY, THE CAR BEGAN TO SURGE, RPMS SKYROCKETED AND CAR BARELY MADE IT UP HILL. SURGING CONTINUED, UNTIL IT BEGAN TO SLIP AND I PULLED OFF THE ROAD AND INTO A SHOPPING CENTER. CAR TOWED TO ESCONDIDO KIA WHO KINDLY GAVE ME A LOANER. NOW BACK IN AZ, I AM TOLD THAT WHEN IT'S FIXED, TRANSPORT TO ME IS UNLIKELY AND IF APPROVED KIA DOES NOT GUARANTEE AGAINST ANY DAMAGE DURING TRANSPORT. ITS A NEW CAR! DUE TO MEDICAL NEEDS HERE, DRIVING 6.5 HOURS THERE AND THEN BACK JUST ISN'T FEASIBLE. KIA DOESNT CARE. I WILL BE OUT OF THIS CAR ASAP AND YOU CAN BET MY NEXT WILL NOT BE A KILLER KIA!
Mfg Campaign: 11406779
Recall Date: Apr 6, 2021
Kia America, Inc.
Defect Description:
POWER TRAIN
Potential Consequences:
BOUGHT BRAND NEW. AT 32K MILES (4MONTHS AFTER 30KTUNE UP) ENGINE LIGHT CAME ON. TOOK TO EARNHARDT KIA IN PHX. WHO INITIALLY STATED THERE WAS 'SOMETHING BROKEN IN THE TRANSMISSION' AFTER A FEW HOURS THEY THEN STATED THE CAR HAD 'INTERNALLY OVERHEATED AND THERE WAS COMBUSTIBLE GASES IN THE RADIATOR. THE THERMOSTAT NEVER INDICATED OVERHEATING. COOLANT RESERVOIR WAS BONE DRY (AFTER FILLING IT THE DAY BEFORE). AFTER 31 DAYS AT KIA A NEW HEAD GASKET WAS PUT ON.. THOUGH I WAS TOLD THE CAR WAS GETTING A NEW ENGINE. I ASKED THE DEALER ON EACH CALL... WHAT ABOUT THE TRANSMISSION WHEREAS I WAS TOLD KOA WOULD MAKE SURE EVERYTHING WOULD BE FIXED BEFORE RETURNED. CAR WAS RETURNED TO ME ON 2/21. ON 4/1 AFTER DRIVING 380(+/-) MILES FROM PHX TO SAN DIEGO TO SEE MY MARINE DEPLOY, THE CAR BEGAN TO SURGE, RPMS SKYROCKETED AND CAR BARELY MADE IT UP HILL. SURGING CONTINUED, UNTIL IT BEGAN TO SLIP AND I PULLED OFF THE ROAD AND INTO A SHOPPING CENTER. CAR TOWED TO ESCONDIDO KIA WHO KINDLY GAVE ME A LOANER. NOW BACK IN AZ, I AM TOLD THAT WHEN IT'S FIXED, TRANSPORT TO ME IS UNLIKELY AND IF APPROVED KIA DOES NOT GUARANTEE AGAINST ANY DAMAGE DURING TRANSPORT. ITS A NEW CAR! DUE TO MEDICAL NEEDS HERE, DRIVING 6.5 HOURS THERE AND THEN BACK JUST ISN'T FEASIBLE. KIA DOESNT CARE. I WILL BE OUT OF THIS CAR ASAP AND YOU CAN BET MY NEXT WILL NOT BE A KILLER KIA!
Corrective Action:
BOUGHT BRAND NEW. AT 32K MILES (4MONTHS AFTER 30KTUNE UP) ENGINE LIGHT CAME ON. TOOK TO EARNHARDT KIA IN PHX. WHO INITIALLY STATED THERE WAS 'SOMETHING BROKEN IN THE TRANSMISSION' AFTER A FEW HOURS THEY THEN STATED THE CAR HAD 'INTERNALLY OVERHEATED AND THERE WAS COMBUSTIBLE GASES IN THE RADIATOR. THE THERMOSTAT NEVER INDICATED OVERHEATING. COOLANT RESERVOIR WAS BONE DRY (AFTER FILLING IT THE DAY BEFORE). AFTER 31 DAYS AT KIA A NEW HEAD GASKET WAS PUT ON.. THOUGH I WAS TOLD THE CAR WAS GETTING A NEW ENGINE. I ASKED THE DEALER ON EACH CALL... WHAT ABOUT THE TRANSMISSION WHEREAS I WAS TOLD KOA WOULD MAKE SURE EVERYTHING WOULD BE FIXED BEFORE RETURNED. CAR WAS RETURNED TO ME ON 2/21. ON 4/1 AFTER DRIVING 380(+/-) MILES FROM PHX TO SAN DIEGO TO SEE MY MARINE DEPLOY, THE CAR BEGAN TO SURGE, RPMS SKYROCKETED AND CAR BARELY MADE IT UP HILL. SURGING CONTINUED, UNTIL IT BEGAN TO SLIP AND I PULLED OFF THE ROAD AND INTO A SHOPPING CENTER. CAR TOWED TO ESCONDIDO KIA WHO KINDLY GAVE ME A LOANER. NOW BACK IN AZ, I AM TOLD THAT WHEN IT'S FIXED, TRANSPORT TO ME IS UNLIKELY AND IF APPROVED KIA DOES NOT GUARANTEE AGAINST ANY DAMAGE DURING TRANSPORT. ITS A NEW CAR! DUE TO MEDICAL NEEDS HERE, DRIVING 6.5 HOURS THERE AND THEN BACK JUST ISN'T FEASIBLE. KIA DOESNT CARE. I WILL BE OUT OF THIS CAR ASAP AND YOU CAN BET MY NEXT WILL NOT BE A KILLER KIA!
Additional Notes:
BOUGHT BRAND NEW. AT 32K MILES (4MONTHS AFTER 30KTUNE UP) ENGINE LIGHT CAME ON. TOOK TO EARNHARDT KIA IN PHX. WHO INITIALLY STATED THERE WAS 'SOMETHING BROKEN IN THE TRANSMISSION' AFTER A FEW HOURS THEY THEN STATED THE CAR HAD 'INTERNALLY OVERHEATED AND THERE WAS COMBUSTIBLE GASES IN THE RADIATOR. THE THERMOSTAT NEVER INDICATED OVERHEATING. COOLANT RESERVOIR WAS BONE DRY (AFTER FILLING IT THE DAY BEFORE). AFTER 31 DAYS AT KIA A NEW HEAD GASKET WAS PUT ON.. THOUGH I WAS TOLD THE CAR WAS GETTING A NEW ENGINE. I ASKED THE DEALER ON EACH CALL... WHAT ABOUT THE TRANSMISSION WHEREAS I WAS TOLD KOA WOULD MAKE SURE EVERYTHING WOULD BE FIXED BEFORE RETURNED. CAR WAS RETURNED TO ME ON 2/21. ON 4/1 AFTER DRIVING 380(+/-) MILES FROM PHX TO SAN DIEGO TO SEE MY MARINE DEPLOY, THE CAR BEGAN TO SURGE, RPMS SKYROCKETED AND CAR BARELY MADE IT UP HILL. SURGING CONTINUED, UNTIL IT BEGAN TO SLIP AND I PULLED OFF THE ROAD AND INTO A SHOPPING CENTER. CAR TOWED TO ESCONDIDO KIA WHO KINDLY GAVE ME A LOANER. NOW BACK IN AZ, I AM TOLD THAT WHEN IT'S FIXED, TRANSPORT TO ME IS UNLIKELY AND IF APPROVED KIA DOES NOT GUARANTEE AGAINST ANY DAMAGE DURING TRANSPORT. ITS A NEW CAR! DUE TO MEDICAL NEEDS HERE, DRIVING 6.5 HOURS THERE AND THEN BACK JUST ISN'T FEASIBLE. KIA DOESNT CARE. I WILL BE OUT OF THIS CAR ASAP AND YOU CAN BET MY NEXT WILL NOT BE A KILLER KIA!
Mfg Campaign: 11406779
Recall Date: Apr 6, 2021
Kia America, Inc.
Defect Description:
POWER TRAIN
Potential Consequences:
WHILE DRIVING ON THE FREEWAY AT 70 MPH, THE VEHICLE BEGAN TO 'SURGE,' THE RPM VARYING ERRATICALLY BETWEEN 2000-3000 RPM. WE GOT OFF THE HIGHWAY AND STOPPED AT A LIGHT'WHEN THE LIGHT TURNED GREEN, I PRESSED THE ACCELERATOR AND THE ENGINE ACCELERATED BUT THE CAR REMAINED STATIONARY. FINALLY, WITH THE RPM AT ABOUT 4000, WE WERE ABLE TO SLOWLY DRIVE INTO A PARKING LOT. NO CHECK ENGINE LIGHT. WE GOT A TOW TO THE NEAREST DEALER. THE SERVICE DEPT ANALYZED THE PROBLEM, AND SAID WE NEEDED A NEW TRANSMISSION. THE NEW 'SOFT' DATE TO RECEIVE THE TRANSMISSION IS 13 APR, ALMOST SIX WEEKS AFTER THE ORIGINAL TRANSMISSION FAILURE ON 2 MAR. THE CAR HAS LESS THAN 3000 MILES ON IT.
Corrective Action:
WHILE DRIVING ON THE FREEWAY AT 70 MPH, THE VEHICLE BEGAN TO 'SURGE,' THE RPM VARYING ERRATICALLY BETWEEN 2000-3000 RPM. WE GOT OFF THE HIGHWAY AND STOPPED AT A LIGHT'WHEN THE LIGHT TURNED GREEN, I PRESSED THE ACCELERATOR AND THE ENGINE ACCELERATED BUT THE CAR REMAINED STATIONARY. FINALLY, WITH THE RPM AT ABOUT 4000, WE WERE ABLE TO SLOWLY DRIVE INTO A PARKING LOT. NO CHECK ENGINE LIGHT. WE GOT A TOW TO THE NEAREST DEALER. THE SERVICE DEPT ANALYZED THE PROBLEM, AND SAID WE NEEDED A NEW TRANSMISSION. THE NEW 'SOFT' DATE TO RECEIVE THE TRANSMISSION IS 13 APR, ALMOST SIX WEEKS AFTER THE ORIGINAL TRANSMISSION FAILURE ON 2 MAR. THE CAR HAS LESS THAN 3000 MILES ON IT.
Additional Notes:
WHILE DRIVING ON THE FREEWAY AT 70 MPH, THE VEHICLE BEGAN TO 'SURGE,' THE RPM VARYING ERRATICALLY BETWEEN 2000-3000 RPM. WE GOT OFF THE HIGHWAY AND STOPPED AT A LIGHT'WHEN THE LIGHT TURNED GREEN, I PRESSED THE ACCELERATOR AND THE ENGINE ACCELERATED BUT THE CAR REMAINED STATIONARY. FINALLY, WITH THE RPM AT ABOUT 4000, WE WERE ABLE TO SLOWLY DRIVE INTO A PARKING LOT. NO CHECK ENGINE LIGHT. WE GOT A TOW TO THE NEAREST DEALER. THE SERVICE DEPT ANALYZED THE PROBLEM, AND SAID WE NEEDED A NEW TRANSMISSION. THE NEW 'SOFT' DATE TO RECEIVE THE TRANSMISSION IS 13 APR, ALMOST SIX WEEKS AFTER THE ORIGINAL TRANSMISSION FAILURE ON 2 MAR. THE CAR HAS LESS THAN 3000 MILES ON IT.
Mfg Campaign: 11405740
Recall Date: Mar 31, 2021
Kia America, Inc.
Defect Description:
STEERING
Potential Consequences:
THE STEERING WHEEL OF MY KIA SOUL 2020 HAMMER. I WAS UNABLE TO START THE CAR AS THE STEERING WHEN BECAME STUCK..JAMMED. CALLED A TOWN TRUCK TO TOWED INTO THE KIA DEALER FOR REPAIRS.
Corrective Action:
THE STEERING WHEEL OF MY KIA SOUL 2020 HAMMER. I WAS UNABLE TO START THE CAR AS THE STEERING WHEN BECAME STUCK..JAMMED. CALLED A TOWN TRUCK TO TOWED INTO THE KIA DEALER FOR REPAIRS.
Additional Notes:
THE STEERING WHEEL OF MY KIA SOUL 2020 HAMMER. I WAS UNABLE TO START THE CAR AS THE STEERING WHEN BECAME STUCK..JAMMED. CALLED A TOWN TRUCK TO TOWED INTO THE KIA DEALER FOR REPAIRS.
Mfg Campaign: 11405777
Recall Date: Mar 31, 2021
Kia America, Inc.
Defect Description:
ENGINE
Potential Consequences:
BOUGHT THE CAR IN AUGUST OF 2019 WHEN THE 2020 MODEL WAS FIRST RELEASED. AROUND 20,000 MILES STARTED TO EXPERIENCE A HEAVY STUTTER IN THE ENGINE AT LOW RPMS. EVENTUALLY IT PROGRESSED OVER ABOUT A WEEK, AND THE CAR WOULD DIE AT A STOP LIGHT/SIGN. WHEN PARKED IT DIES AT RANDOM, YOU CAN HEAR AND FEEL THE ENGINE STRUGGLE. IF YOU WATCH THE RPMS YOU CAN SEE IT VISIBLY FLUCTUATING, BETWEEN ABOUT 500 AND 800 RPM'S THEN AT RANDOM IT WILL BOG HARD AND DIE. IF YOU KICK ON THE A/C WHILE STOPPED, YOU CAN WATCH IT BOG, WHICH ABOUT 100-200 RPMS IS NORMAL THEN IT SHOULD IDLE UP AGAIN. HOWEVER IT BOGS ABOUT 500 RPMS AND WILL SOMETIMES DIE. I WANTED THE ALTERNATOR, AND COMPRESSOR CHECKED. TOOK IT TO KALIDY KIA IN EDMOND OKLAHOMA AND THEY TOLD ME MULTIPLE TIMES THERE WAS NOTHING WRONG WITH IT OR THAT THE INTAKE VALVE WAS DIRTY, WHICH AT 20,000 MILES IS RIDICULOUS. TOLD ME I WAS USING BAD GAS, AND STILL TO THIS DAY WON'T LOOK INTO THE PROBLEM EVEN UNDER WARRANTY. NO TELLING WHEN IT IS GOING TO HAPPEN.
Corrective Action:
BOUGHT THE CAR IN AUGUST OF 2019 WHEN THE 2020 MODEL WAS FIRST RELEASED. AROUND 20,000 MILES STARTED TO EXPERIENCE A HEAVY STUTTER IN THE ENGINE AT LOW RPMS. EVENTUALLY IT PROGRESSED OVER ABOUT A WEEK, AND THE CAR WOULD DIE AT A STOP LIGHT/SIGN. WHEN PARKED IT DIES AT RANDOM, YOU CAN HEAR AND FEEL THE ENGINE STRUGGLE. IF YOU WATCH THE RPMS YOU CAN SEE IT VISIBLY FLUCTUATING, BETWEEN ABOUT 500 AND 800 RPM'S THEN AT RANDOM IT WILL BOG HARD AND DIE. IF YOU KICK ON THE A/C WHILE STOPPED, YOU CAN WATCH IT BOG, WHICH ABOUT 100-200 RPMS IS NORMAL THEN IT SHOULD IDLE UP AGAIN. HOWEVER IT BOGS ABOUT 500 RPMS AND WILL SOMETIMES DIE. I WANTED THE ALTERNATOR, AND COMPRESSOR CHECKED. TOOK IT TO KALIDY KIA IN EDMOND OKLAHOMA AND THEY TOLD ME MULTIPLE TIMES THERE WAS NOTHING WRONG WITH IT OR THAT THE INTAKE VALVE WAS DIRTY, WHICH AT 20,000 MILES IS RIDICULOUS. TOLD ME I WAS USING BAD GAS, AND STILL TO THIS DAY WON'T LOOK INTO THE PROBLEM EVEN UNDER WARRANTY. NO TELLING WHEN IT IS GOING TO HAPPEN.
Additional Notes:
BOUGHT THE CAR IN AUGUST OF 2019 WHEN THE 2020 MODEL WAS FIRST RELEASED. AROUND 20,000 MILES STARTED TO EXPERIENCE A HEAVY STUTTER IN THE ENGINE AT LOW RPMS. EVENTUALLY IT PROGRESSED OVER ABOUT A WEEK, AND THE CAR WOULD DIE AT A STOP LIGHT/SIGN. WHEN PARKED IT DIES AT RANDOM, YOU CAN HEAR AND FEEL THE ENGINE STRUGGLE. IF YOU WATCH THE RPMS YOU CAN SEE IT VISIBLY FLUCTUATING, BETWEEN ABOUT 500 AND 800 RPM'S THEN AT RANDOM IT WILL BOG HARD AND DIE. IF YOU KICK ON THE A/C WHILE STOPPED, YOU CAN WATCH IT BOG, WHICH ABOUT 100-200 RPMS IS NORMAL THEN IT SHOULD IDLE UP AGAIN. HOWEVER IT BOGS ABOUT 500 RPMS AND WILL SOMETIMES DIE. I WANTED THE ALTERNATOR, AND COMPRESSOR CHECKED. TOOK IT TO KALIDY KIA IN EDMOND OKLAHOMA AND THEY TOLD ME MULTIPLE TIMES THERE WAS NOTHING WRONG WITH IT OR THAT THE INTAKE VALVE WAS DIRTY, WHICH AT 20,000 MILES IS RIDICULOUS. TOLD ME I WAS USING BAD GAS, AND STILL TO THIS DAY WON'T LOOK INTO THE PROBLEM EVEN UNDER WARRANTY. NO TELLING WHEN IT IS GOING TO HAPPEN.
Mfg Campaign: 11405860
Recall Date: Mar 31, 2021
Kia America, Inc.
Defect Description:
ELECTRICAL SYSTEM
Potential Consequences:
MY KIA SOUL 2020, THE ENGINE LIGHTS CAME UP, THE PARKING LIGHTS, THE RIGHT HEADLIGHTS, THE REAR BACK RIGHT SIGNAL LIGHTS, THE FUEL SYSTEM AND THE BREAKS SYSTEM ALL OF THEM MALFUNCTIONED. THE DEALER CHARGED FOR THE REPAIRS.
Corrective Action:
MY KIA SOUL 2020, THE ENGINE LIGHTS CAME UP, THE PARKING LIGHTS, THE RIGHT HEADLIGHTS, THE REAR BACK RIGHT SIGNAL LIGHTS, THE FUEL SYSTEM AND THE BREAKS SYSTEM ALL OF THEM MALFUNCTIONED. THE DEALER CHARGED FOR THE REPAIRS.
Additional Notes:
MY KIA SOUL 2020, THE ENGINE LIGHTS CAME UP, THE PARKING LIGHTS, THE RIGHT HEADLIGHTS, THE REAR BACK RIGHT SIGNAL LIGHTS, THE FUEL SYSTEM AND THE BREAKS SYSTEM ALL OF THEM MALFUNCTIONED. THE DEALER CHARGED FOR THE REPAIRS.
Mfg Campaign: 11405292
Recall Date: Mar 29, 2021
Need Legal Help?
Featured Attorneys
Barry Edzant
Edzant Price LLC
Valencia, CA • 36 yrs
Focus: Lemon Law, Personal Injury